Relay-Version: version B 2.10 5/3/83; site utzoo.UUCP Posting-Version: version B 2.10.1 6/24/83; site ssc-vax.UUCP Path: utzoo!linus!decvax!ittvax!dcdwest!sdcsvax!sdcrdcf!hplabs!tektronix!uw-beaver!ssc-vax!alcmist From: alcmist@ssc-vax.UUCP Newsgroups: net.rec.skydive Subject: lodestar crash repost Message-ID: <150@ssc-vax.UUCP> Date: Thu, 17-May-84 11:42:40 EDT Article-I.D.: ssc-vax.150 Posted: Thu May 17 11:42:40 1984 Date-Received: Tue, 22-May-84 01:06:13 EDT Organization: Boeing Aerospace, Seattle Lines: 22 Today in Washington the National Transportation Safety Board released their findings about the August 1983 crash of a Lockheed Learstar jumpship which killed 9 jumpers and 2 pilots. To summarize, they said the crash was caused by the failure of the operator of the aircraft and the pilot in command to review the effect that the jumpers' exit lineup would have on the aircraft's center of gravity. The NTSB concluded that the plane went out of control because it was too tailheavy to be controllable. The NTSB also faulted the FAA district office for insufficient surveilance of the jump operation, and recommended that FAA people keep a closer watch on parachuting operations in the future. I will try to get hold of a copy of their report, and will post details if anyone is interested. The above is a summary of the findings of the National Transportation Safety Board and does not reflect the opinions of Boeing, the staff of the software support center VAX, or myself. -fred wamsley, (206) 773-4200